Market Notices

58395POWER SYSTEM EVENTS18/04/2017 12:43:07 PM

Non-credible contingency event - Vic region - 18/04/17

AEMO ELECTRICITY MARKET NOTICE

Non-credible contingency event - Vic region - 18/04/17

Update to AEMO Electricity Market Notice 58394

At 1107 hrs the Moorabool - Mortlake 500 kV Line tripped at the Moorabool end only.
At 1110 hrs the Moorabool - Mortlake 500 kV Line was manually de-energised by opening at the Mortlake end.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.

Manager NEM Real Time Operations
58391POWER SYSTEM EVENTS15/04/2017 08:10:36 PM

Update - Non-credible contingency event - NSW Region - 15 Apr 2017

AEMO ELECTRICITY MARKET NOTICE


Update - Non-credible contingency event - NSW Region - 15 Apr 2017

Refer Market Notice 58390

At 1644 hrs the Broken Hill No 2 220/22 kV Transformer and No 2 Section 22 kV Bus tripped. This equipment has been returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.


Manager NEM Real Time Operations
58390POWER SYSTEM EVENTS15/04/2017 05:59:50 PM

Non-credible contingency event - NSW Region - 15 Apr 2017

AEMO ELECTRICITY MARKET NOTICE

Non-credible contingency event - NSW Region - 15 Apr 2017

At 1644 hrs the Broken Hill No 2 220/22 kV Transformer and No 2 Section 22 kV Bus tripped.

(Also subsequent loss of Broken Hill Solar Farm)

AEMO did not instruct load shedding.

AEMO has been advised of disconnection of 14 MW of bulk electrical load.


The cause of this non credible contingency event is not known at this stage and is still under investigation.

The Bus and Transformer are still out of service


Manager NEM Real Time Operations
58335POWER SYSTEM EVENTS04/04/2017 03:35:48 PM

Update- Non-credible contingency event - Qld Region - 04/04/2017

AEMO ELECTRICITY MARKET NOTICE


Update- Non-credible contingency event - Qld Region - 04/04/2017

Refer Market Notice 58331

At 0307 hrs trip of the Murarrie No.1 110 kV Bus coincident with trip of 7270 Murarrie - Lytton Bulk Supply 110 kV Line.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.


Manager NEM Real Time Operations

58331POWER SYSTEM EVENTS04/04/2017 04:50:37 AM

Non-credible contingency event - Qld Region - 04/04/2017

AEMO ELECTRICITY MARKET NOTICE


Non-credible contingency event - Qld Region - 04/04/2017

At 0307 hrs trip of the Murarrie No.1 110 kV Bus coincident with trip of 7270 Murarrie - Lytton Bulk Supply 110 kV Line.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
58287POWER SYSTEM EVENTS29/03/2017 09:59:48 AM

Update - Non-credible contingency event - Qld region - 29/03/17

AEMO ELECTRICITY MARKET NOTICE

Refer AEMO Electricity Market Notice 58285

At 0840 hrs 29/03/17 the Mudgeeraba No. 2 and No. 4 110 kV Bus tripped.
The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
58285POWER SYSTEM EVENTS29/03/2017 09:14:04 AM

Non-credible contingency event - Qld region - 29/03/17

AEMO ELECTRICITY MARKET NOTICE

Non-credible contingency event - Qld region - 29/03/17

At 0840 hrs 29/03/17 the Mudgeeraba No. 2 and No. 4 110 kV Bus tripped. This bus trip also tripped Mudgeeraba - Terranora No. 758 110 kV Line which interrupted supply to Terranora substation.
Note: Mudgeeraba - Terranora No. 757 110 kV Line was out of service (planned outage)
AEMO did not instruct load shedding.
The interruption to supply at Terranora substation resulted in approximately 35 MW of load lost.
The cause of this non credible contingency event is not known at this stage.

Manager NEM Real Time Operations
58255POWER SYSTEM EVENTS27/03/2017 07:01:29 PM

Non-credible contingency event - NSW Region - 27/03/2017

AEMO ELECTRICITY MARKET NOTICE


Non-credible contingency event - NSW Region - 27/03/2017

At 1828 hrs the Cooma-Williamsdale 97D 132 kV Line opened at the Williamsdale end only.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
58240POWER SYSTEM EVENTS26/03/2017 11:23:08 AM

Non-credible contingency event - Vic Region - 26 Mar 2017

AEMO ELECTRICITY MARKET NOTICE

Non-credible contingency event - Vic Region - 26 Mar 2017

At 1056 hrs the Dederang - Sth Morang No 1 330 kV Line opened at the Sth Morang end only.

The Line was placed on load at 1100 hrs
AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
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