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Non-credible contingency event - Qld region - 23/05/2023
Non-credible contingency event - Qld region - 23/05/2023
At 2106 hrs the Kamerunga - Woree 7141 132 kV Line and Barron Gorge 1 and 2 generating units tripped. At 2107 hrs the Kamerunga - Barron Gorge 7143 132 kV Line tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Update - Non-credible contingency event - Qld region - 16/05/2023
Refer AEMO ELECTRICITY MARKET NOTICE MN107943
At 2142 hrs the H3 Belmont No 2 275 kV bus was returned to service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - Qld region - 16/05/2023
Non-credible contingency event - Qld region - 16/05/2023
At 1852 hrs the H3 Belmont No 2 275 kV bus tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Update - Non-credible contingency event - NSW region - 07/04/2023
Update - Non-credible contingency event - NSW region - 07/04/2023
Refer AEMO MN 107349
At 1648 hrs 18/04/2023, the Tamworth SVC was returned to service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - NSW region - 07/04/2023
Non-credible contingency event - NSW region - 07/04/2023
At 2257 hrs the Liddell - Tomago 82 330 kV line and the Tamworth SVC tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Non-credible contingency event - NSW region - 07/04/2023
Refer MN 107334 - Non-credible contingency event more likely to occur due to existence of abnormal condition/s - NSW region.
Non-credible contingency event - NSW region - 07/04/2023
At 1828 hrs the Mt Piper - Bannaby 5A6 500 kV line and Mt Piper - Bannaby 5A7 500 kV line tripped and auto reclosed.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
Manager NEM Real Time Operations
Non-credible contingency event - SA region - 06/04/2023
Non-credible contingency event - SA region - 06/04/2023
At 1814 hrs the Robertstown - North West Bend No 1 Line and the North West Bend - Monash - Berri No 1 Line tripped and auto reclosed.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Tasmanian Regulation FCAS changes - Wednesday 5th April 2023
AEMO are changing the procurement of Regulation FCAS for the TAS region.
This change is based on advice received from TasNetworks, following a review of operation of the TAS region with the end of the reclassification of Basslink.
Refer to AEMO Electricity market notice 105443.
Following this change Regulation FCAS requirements for the TAS region will only be procured from within TAS.
This change will be implemented from 1000 on Wed 5th April.
Ben Blake
Manager Congestion & Grid Modelling
Non-credible contingency event - Qld region - 01/04/2023
Non-credible contingency event - Qld region - 01/04/2023
At 1950 hrs 01/04/2023 there was an unplanned outage of Unit 5 and Unit 7 at H48 Braemar 2 Power Station.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations