Market Notices

53526POWER SYSTEM EVENTS26/05/2016 09:14:35 AM

Non-credible contingency event - SA region - 26/05/2016

AEMO ELECTRICITY MARKET NOTICE

Non-credible contingency event - SA region - 26/05/2016

At 0851 hrs the South East Tailem Bend No. 1 275 kV Line and the South East No. 1 275 kV SVC tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.


The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
53516POWER SYSTEM EVENTS24/05/2016 06:57:10 PM

Update Non-credible contingency event - NSW region - 24 May 2016

AEMO ELECTRICITY MARKET NOTICE

Update Non-credible contingency event - NSW region - 24 May 2016

Refer market notice 53511,53515

At 0950 hrs the Tuggerah 330kV circuit breakers 212A and 2M2A opened simultaneously.

At 1827 hrs the Tuggerah 330kV circuit breakers 212A and 2M2A were returned to service.

The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.


Manager NEM Real Time Operations
53515POWER SYSTEM EVENTS24/05/2016 03:24:22 PM

Update Non-credible contingency event - NSW region - 24 May 2016

AEMO ELECTRICITY MARKET NOTICE

Update Non-credible contingency event - NSW region - 24 May 2016

Refer market notice 53511

At 0950 hrs the Tuggerah 330kV circuit breakers 212A and 2M2A opened simultaneously.

The cause of this non credible contingency event is not known at this stage.

Refer to AEMO Network Outage Scheduler (NOS) for further details.

Manager NEM Real Time Operations
53511POWER SYSTEM EVENTS24/05/2016 11:16:38 AM

Non-credible contingency event - NSW region - 24 May 2016

AEMO ELECTRICITY MARKET NOTICE

Non-credible contingency event - NSW region - 24 May 2016

At 0950 hrs the Tuggerah 330kV circuit breakers 212A and 2M2A opened simultaneously.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
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