Market Notices

116072POWER SYSTEM EVENTS10/04/2024 09:08:03 AM

Non-credible contingency event - QLD region - 10/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - QLD region - 10/04/2024

At 0730 hrs the Ingham South to Cardwell 132 kV line tripped at the Ingham South end only.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.

Manager NEM Real Time Operations
     
116052GENERAL NOTICE09/04/2024 11:26:28 AM

Increase to QNI limit to next hold point of 850 MW NSW to Qld

AEMO ELECTRICITY MARKET NOTICE

Refer to market notices 114742.

AEMO, TransGrid, Powerlink have reviewed the test results following the QNI minor testing on 15th February 2024. The next hold point can now be released.

The hold point of 850 MW from NSW to Qld will be implemented as of 1000 hrs 10th April 2024.

Please also refer to the published formal QNI minor testing information at the following link:
https://www.aemo.com.au/consultations/current-and-closed-consultations/qld-to-nsw-interconnector-qni-upgrade

Ben Blake
AEMO Operations
     
115975POWER SYSTEM EVENTS05/04/2024 06:57:00 PM

Update - Non-credible contingency event - SA region - 25/03/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - SA region - 25/03/2024

Refer AEMO Electricity Market Notice 115794

At 1736 hrs Torrens Island BC3 275 kV CB was returned to service.
Torrens Island BW3 275 kV CB and Torrens Island - Lefevre 275 kV line previously returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
     
115974GENERAL NOTICE09/04/2024 06:18:24 PM

Update - Network Augmentation Commissioned - QLD Region - 09/04/2024

AEMO ELECTRICITY MARKET NOTICE

Update - Network Augmentation Commissioned - QLD Region - 09/04/2024

Refer Market notice: 115957

Guybal Munjan 275 kV Switching Station has been cut into the existing Ross - Chalumbin No.858 275 kV line to form the following circuits:

H93 Guybal Munjan - H32 Chalumbin No.858 275 kV line
H13 Ross - H93 Guybal Munjan No.8916 275 kV line

Manager NEM Real Time Operations
     
115957GENERAL NOTICE04/04/2024 02:36:06 PM

Network Augmentation Commissioned - QLD Region - 04/04/2024

AEMO ELECTRICITY MARKET NOTICE

Network Augmentation Commissioned - QLD Region - 04/04/2024

Commissioned:

H93 Guybal Munjan 275 kV Switching Station
H13 Ross - H93 Guybal Munjan No.8916 275 kV line

Manager NEM Real Time Operations
     
115948POWER SYSTEM EVENTS03/04/2024 11:45:55 PM

Non-credible contingency event - QLD region - 03/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - QLD region - 03/04/2024

At 2322 hrs the Kareeya PS units 1, 2, 3 and 4 tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.


The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
     
115947POWER SYSTEM EVENTS03/04/2024 11:16:35 PM

Update - Non-credible contingency event - NSW region - 03/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - NSW region - 03/04/2024

Refer AEMO Electricity Market Notice 115944

At 2301 hrs the Eraring Power Station Unit 1 and Unit 2 were returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
     
115944POWER SYSTEM EVENTS03/04/2024 02:21:43 PM

Non-credible contingency event - NSW region - 03/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - NSW region - 03/04/2024

At 1322 hrs the Eraring Power Station Unit 1 and the Eraring Power Station Unit 2 tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
     
115919INTER-REGIONAL TRANSFER02/04/2024 07:43:53 AM

Inter-regional transfer limit variation - Pelican Point to Parafield Gardens West 275kV Line - SA region - 02/04/2024

AEMO ELECTRICITY MARKET NOTICE

Inter-regional transfer limit variation - Pelican Point to Parafield Gardens West 275kV Line - SA region - 02/04/2024

A planned outage of Pelican Point to Parafield Gardens West 275kV Line in the SA region was scheduled from 0730 hrs 02/04/2024 to 1530 hrs 02/04/2024.

The outage has been cancelled at 0718 hrs 02/04/2024

Constraint set(s) revoked: S-PGPP, S-PPPG_PELPT

This constraint set(s) contains equations with the following interconnectors on the LHS.
V-SA

Refer to the AEMO Network Outage Scheduler for further information.

Manager NEM Real Time Operations
     
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