Market Notices

116162POWER SYSTEM EVENTS17/04/2024 06:10:18 AM

Update - Non-credible contingency event - VIC region - 17/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - VIC region - 17/04/2024

Refer AEMO Electricity Market Notice 116160

At 0610 hrs the Heywood No 2 500 kV bus was returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
     
116160POWER SYSTEM EVENTS17/04/2024 04:29:44 AM

Non-credible contingency event - VIC region - 17/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - VIC region - 17/04/2024

At 0414 hrs the Heywood No 2 500 kV bus tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
     
116098POWER SYSTEM EVENTS12/04/2024 01:39:23 PM

Update - Non-credible contingency event - TAS region - 12/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - TAS region - 12/04/2024

Refer AEMO Electricity Market Notice 116095

At 1304 hrs the Sheffield - Farrell No.2 220 kV line was returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
     
116095POWER SYSTEM EVENTS12/04/2024 11:22:09 AM

Non-credible contingency event - TAS region - 12/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - TAS region - 12/04/2024

At 1048 hrs the Sheffield - Farrell No.2 220 kV line tripped during restoration due to fault on the line.

AEMO did not instruct load shedding.

AEMO has been advised of disconnection of major industrial load approximately 550 MW.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
     
116078POWER SYSTEM EVENTS10/04/2024 03:44:19 PM

Update - Non-credible contingency event - QLD region - 10/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - QLD region - 10/04/2024

Refer AEMO Electricity Market Notice 116072

At 1540 hrs the Ingham South to Cardwell 132 kV line was returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
     
116072POWER SYSTEM EVENTS10/04/2024 09:08:03 AM

Non-credible contingency event - QLD region - 10/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - QLD region - 10/04/2024

At 0730 hrs the Ingham South to Cardwell 132 kV line tripped at the Ingham South end only.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.

Manager NEM Real Time Operations
     
115975POWER SYSTEM EVENTS05/04/2024 06:57:00 PM

Update - Non-credible contingency event - SA region - 25/03/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - SA region - 25/03/2024

Refer AEMO Electricity Market Notice 115794

At 1736 hrs Torrens Island BC3 275 kV CB was returned to service.
Torrens Island BW3 275 kV CB and Torrens Island - Lefevre 275 kV line previously returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
     
115948POWER SYSTEM EVENTS03/04/2024 11:45:55 PM

Non-credible contingency event - QLD region - 03/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - QLD region - 03/04/2024

At 2322 hrs the Kareeya PS units 1, 2, 3 and 4 tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.


The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
     
115947POWER SYSTEM EVENTS03/04/2024 11:16:35 PM

Update - Non-credible contingency event - NSW region - 03/04/2024

AEMO ELECTRICITY MARKET NOTICE.

Update - Non-credible contingency event - NSW region - 03/04/2024

Refer AEMO Electricity Market Notice 115944

At 2301 hrs the Eraring Power Station Unit 1 and Unit 2 were returned to service.

The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

AEMO will not reclassify this event as a credible contingency event.

Manager NEM Real Time Operations
     
X
Cookies help us improve your website experience.
By using our website, you agree to our use of cookies.
Confirm