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Update - Non-credible contingency event - Queensland region
Refer to Market Notice 63309
Update - Non-credible contingency event - Queensland region
The cause of the Calliope River - Gin Gin (814) 275kV Transmission Line trip has been identified and isolated.
The line was returned to service at 1607 hrs 02/07/2018
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - Queenslad region
Non-credible contingency event - Queenslad region
At 0755 hrs 02/07/2018 during planned switching at Calliope River substation the Calliope River - Gin Gin (814) 275kV Transmission Line tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage and the line remains out of service.
Manager NEM Real Time Operations
Non-credible contingency event - NSW region - 21/06/2018
Non-credible contingency event - NSW region - 21/06/2018
At 1718 hrs the 996 Wagga 330 - ANM tee Morven 132 kV line tripped at the Wagga end only.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - Queensland region
Non-credible contingency event - Queensland region
At 0806hrs the H40 Wurdong No 1 275 kV bus tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - Vic region - 14/06/18
At 0126 hrs the APD Potline 1 and the APD Potline 2 tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Non-credible contingency event - Vic region - 28/05/2018
Non-credible contingency event - Vic region - 28/05/2018
At 2221 hrs the Rowville to Templestowe 220 kV Line tripped at the Templestowe end only. The line was returned to service at 2310 hrs.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Update Non-credible contingency event - QLD region -26/05/2018
Update - Non-credible contingency event -QLD region -26/05/2018
Update to MN 62950.
At 0934 hrs at the H35 Strathmore substation the No.1 and No.2 132 kV Buses tripped out of service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
Therefore AEMO has cancelled this event as being a credible contingency event from 1925 Hrs 26/05/2018
Manager NEM Real Time Operations
Non-credible contingency event - QLD region -26/05/2018
Non-credible contingency event -QLD region -26/05/2018
At 0934 hrs at the H35 Strathmore substation the No.1 and No.2 132 kV Buses tripped.
AEMO did not instruct load shedding. AEMO has not been advised of any loss of load.
The cause of this non credible contingency event is not known at this stage.
AEMO is not satisfied that this non credible event is unlikely to re-occur.
AEMO therefore classifies this event as being a credible contingency event.
Manager NEM Real Time Operations
Update - Non-credible contingengency event - QLD region -22/05/2018
Update - Non-credible contingengency event -QLD region -22/05/2018
Update to MN 62895.
At 1001 hrs at the Ross substation 275/132kV #2 #3 #4Transformers and SVC tripped out of service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations